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Message-Id: <1E6A718E-ABEA-4B68-9A5A-C34880273550@holtmann.org>
Date: Sat, 19 Oct 2019 21:19:40 +0200
From: Marcel Holtmann <marcel@...tmann.org>
To: Matthias Kaehlcke <mka@...omium.org>
Cc: Jeffrey Hugo <jeffrey.l.hugo@...il.com>,
Johan Hedberg <johan.hedberg@...il.com>,
c-hbandi@...eaurora.org, bgodavar@...eaurora.org,
linux-bluetooth@...r.kernel.org,
MSM <linux-arm-msm@...r.kernel.org>,
lkml <linux-kernel@...r.kernel.org>
Subject: Re: [PATCH] Bluetooth: hci_qca: Add delay for wcn3990 stability
Hi Matthias,
>>>>>> On the msm8998 mtp, the response to the baudrate change command is never
>>>>>> received. On the Lenovo Miix 630, the response to the baudrate change
>>>>>> command is corrupted - "Frame reassembly failed (-84)".
>>>>>>
>>>>>> Adding a 50ms delay before re-enabling flow to receive the baudrate change
>>>>>> command response from the wcn3990 addesses both issues, and allows
>>>>>> bluetooth to become functional.
>>>>>
>>>>> From my earlier debugging on sdm845 I don't think this is what happens.
>>>>> The problem is that the wcn3990 sends the response to the baudrate change
>>>>> command using the new baudrate, while the UART on the SoC still operates
>>>>> with the prior speed (for details see 2faa3f15fa2f ("Bluetooth: hci_qca:
>>>>> wcn3990: Drop baudrate change vendor event"))
>>>>>
>>>>> IIRC the 50ms delay causes the HCI core to discard the received data,
>>>>> which is why the "Frame reassembly failed" message disappears, not
>>>>> because the response was received. In theory commit 78e8fa2972e5
>>>>> ("Bluetooth: hci_qca: Deassert RTS while baudrate change command")
>>>>> should have fixed those messages, do you know if CTS/RTS are connected
>>>>> on the Bluetooth UART of the Lenovo Miix 630?
>>>>
>>>> I was testing with 5.4-rc1 which contains the indicated RTS fix.
>>>>
>>>> Yes, CTS/RTS are connected on the Lenovo Miix 630.
>>>>
>>>> I added debug statements which indicated that data was received,
>>>> however it was corrupt, and the packet type did not match what was
>>>> expected, hence the frame reassembly errors.
>>>
>>> Do you know if any data is received during the delay? In theory that
>>> shouldn't be the case since RTS is deasserted, just double-checking.
>>
>> I don't think so, but I've run so many tests, I'm not 100% positive.
>> Let me go double check and get back to you.
>>
>>>
>>> What happens if you add a longer delay (e.g. 1s) before/after setting
>>> the host baudrate?
>>
>> Hmm, not exactly sure. I will test.
>>
>>>
>>>> In response to this patch, Balakrishna pointed me to a bug report
>>>> which indicated that some of the UART GPIO lines need to have a bias
>>>> applied to prevent errant data from floating lines -
>>>>
>>>> https://chromium-review.googlesource.com/c/chromiumos/third_party/kernel/+/1391888
>>>
>>> Yeah, that was another source of frame reassembly errors that we were
>>> seeing on SDM845.
>>>
>>> Balakrishna, please post these kind of replies on-list, so that
>>> everybody can benefit from possible solutions or contribute to the
>>> discussion.
>>>
>>>> It turns out this fix was never applied to msm8998. Applying the fix
>>>> does cause the the frame reassembly errors to go away, however then
>>>> the host SoC never receives the baud rate change response (I increased
>>>> the timeout from 2faa3f15fa2f ("Bluetooth: hci_qca: wcn3990: Drop
>>>> baudrate change vendor event") to 5 seconds). As of now, this patch
>>>> is still required.
>>>
>>> Interesting.
>>>
>>> FTR, this is the full UART pin configuration for cheza (SDM845):
>>>
>>> &qup_uart6_default {
>>> /* Change pinmux to all 4 pins since CTS and RTS are connected */
>>> pinmux {
>>> pins = "gpio45", "gpio46",
>>> "gpio47", "gpio48";
>>> };
>>>
>>> pinconf-cts {
>>> /*
>>> * Configure a pull-down on 45 (CTS) to match the pull of
>>> * the Bluetooth module.
>>> */
>>> pins = "gpio45";
>>> bias-pull-down;
>>> };
>>>
>>> pinconf-rts-tx {
>>> /* We'll drive 46 (RTS) and 47 (TX), so no pull */
>>> pins = "gpio46", "gpio47";
>>> drive-strength = <2>;
>>> bias-disable;
>>> };
>>>
>>> pinconf-rx {
>>> /*
>>> * Configure a pull-up on 48 (RX). This is needed to avoid
>>> * garbage data when the TX pin of the Bluetooth module is
>>> * in tri-state (module powered off or not driving the
>>> * signal yet).
>>> */
>>> pins = "gpio48";
>>> bias-pull-up;
>>> };
>>> };
>>>
>>> Does this correspond to what you tried on the Lenovo Miix 630?
>>
>> Which GPIO maps to which pin is different -
>> 45 - TX
>> 46 - RX
>> 47 - CTS
>> 48 - RFR (RTS)
>>
>> However, accounting for that, yes that corresponds to what I used.
>
> Thanks for re-confirming.
>
>>>> I have no idea why the delay is required, and was hoping that posting
>>>> this patch would result in someone else providing some missing pieces
>>>> to determine the real root cause. I suspect that asserting RTS at the
>>>> wrong time may cause an issue for the wcn3990, but I have no data nor
>>>> documentation to support this guess. I welcome any further insights
>>>> you may have.
>>>
>>> Unfortunately I don't have a clear suggestion at this point, debugging
>>> the original problem which lead to 2faa3f15fa2f ("Bluetooth: hci_qca:
>>> wcn3990: Drop baudrate change vendor event") involved quite some time
>>> and hooking up a scope/logic analyzer ...
>>>
>>> I also suspect RTS is involved, and potentially the configuration of
>>> the pulls. It might be interesting to analyze the data that leads to
>>> the frame assembly error and determine if it is just noise (wrong
>>> pulls/drive strength?) or received with a non-matching baud-rate.
>>
>> I don't have a scope/logic analyzer, but since I hooked up the
>> blsp_bam I'm able to see the raw data from the uart before it gets to
>> the HCI stack or anything. As a side note, having the bam or not
>> seemed to have no effect on the issue.
>
> It's not exactly the same though. I suppose with the blsp_bam you only
> see the actual data when the UART runs at the same speed as it's
> counterpart. With a logic analyzer you can change the speed after
> data capture, which might convert apparent garbage into reasonable
> data.
>
>> Most of the time the data was one byte (zero), some times it was a
>> string of zero bytes. Rarely it would be random data.
>
> In terms of data ss there difference between a string of zero bytes
> and a single zero byte?
>
> From my notes the response (vendor event) to a baudrate change
> command on the WCN3990 is:
>
> 04 0e 04 01 00 00 00
>
> The tail *might* be the zero(s) you are seeing, and the first part gets
> lost for some reason?
you could allow the zero bytes be a valid sequence. See BCM_RECV_NULL for an example on how to include that into the H:4 receive code. Then remove the extra msleep and run btmon to see if you get zero bytes and how many.
Regards
Marcel
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