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Message-ID: <1jlfg7k2ux.fsf@starbuckisacylon.baylibre.com>
Date: Thu, 15 Oct 2020 15:58:30 +0200
From: Jerome Brunet <jbrunet@...libre.com>
To: Ionela Voinescu <ionela.voinescu@....com>
Cc: Jassi Brar <jassisinghbrar@...il.com>,
Kevin Hilman <khilman@...libre.com>,
linux-amlogic@...ts.infradead.org, Da Xue <da@...re.computer>,
linux-kernel@...r.kernel.org
Subject: Re: [PATCH] mailbox: cancel timer before starting it
On Thu 15 Oct 2020 at 15:46, Ionela Voinescu <ionela.voinescu@....com> wrote:
> Hi guys,
>
> On Wednesday 23 Sep 2020 at 14:39:16 (+0200), Jerome Brunet wrote:
>> If the txdone is done by polling, it is possible for msg_submit() to start
>> the timer while txdone_hrtimer() callback is running. If the timer needs
>> recheduling, it could already be enqueued by the time hrtimer_forward_now()
>> is called, leading hrtimer to loudly complain.
>>
>> WARNING: CPU: 3 PID: 74 at kernel/time/hrtimer.c:932 hrtimer_forward+0xc4/0x110
>> CPU: 3 PID: 74 Comm: kworker/u8:1 Not tainted 5.9.0-rc2-00236-gd3520067d01c-dirty #5
>> Hardware name: Libre Computer AML-S805X-AC (DT)
>> Workqueue: events_freezable_power_ thermal_zone_device_check
>> pstate: 20000085 (nzCv daIf -PAN -UAO BTYPE=--)
>> pc : hrtimer_forward+0xc4/0x110
>> lr : txdone_hrtimer+0xf8/0x118
>> [...]
>>
>> Canceling the timer before starting it ensure that the timer callback is
>> not running when the timer is started, solving this race condition.
>>
>> Fixes: 0cc67945ea59 ("mailbox: switch to hrtimer for tx_complete polling")
>> Reported-by: Da Xue <da@...re.computer>
>> Signed-off-by: Jerome Brunet <jbrunet@...libre.com>
>> ---
>> drivers/mailbox/mailbox.c | 8 ++++++--
>> 1 file changed, 6 insertions(+), 2 deletions(-)
>>
>> diff --git a/drivers/mailbox/mailbox.c b/drivers/mailbox/mailbox.c
>> index 0b821a5b2db8..34f9ab01caef 100644
>> --- a/drivers/mailbox/mailbox.c
>> +++ b/drivers/mailbox/mailbox.c
>> @@ -82,9 +82,13 @@ static void msg_submit(struct mbox_chan *chan)
>> exit:
>> spin_unlock_irqrestore(&chan->lock, flags);
>>
>> - if (!err && (chan->txdone_method & TXDONE_BY_POLL))
>> - /* kick start the timer immediately to avoid delays */
>> + if (!err && (chan->txdone_method & TXDONE_BY_POLL)) {
>> + /* Disable the timer if already active ... */
>> + hrtimer_cancel(&chan->mbox->poll_hrt);
>> +
>> + /* ... and kick start it immediately to avoid delays */
>> hrtimer_start(&chan->mbox->poll_hrt, 0, HRTIMER_MODE_REL);
>> + }
>> }
>>
>> static void tx_tick(struct mbox_chan *chan, int r)
>
> I've tracked a regression back to this commit. Details to reproduce:
Hi Ionela,
I don't have access to your platform and I don't get what is going on
from the log below.
Could you please give us a bit more details about what is going on ?
All this patch does is add hrtimer_cancel().
* It is needed if the timer had already been started, which is
appropriate AFAIU
* It is a NO-OP is the timer is not active.
>
>
> - HEAD: (linux-next)
> * 62c04453381e Jerome Brunet 3 weeks ago mailbox: cancel timer before starting it
>
> - Platform: arm64 Juno R0 and Juno R2 [1]
>
> - Partial log:
> [ 0.000000] Booting Linux on physical CPU 0x0000000100 [0x410fd030]
> [ 0.000000] Linux version 5.9.0-rc8-01722-g62c04453381e () (aarch64-none-linux-gnu-gcc (GNU Toolchain for the A-profile Architecture 9.2-2019.12 (arm-9.10)) 9.2.1 20191025, GNU ld (GNU Toolchain for the A-profile Architecture 9.2-2019.12 (arm-9.10)) 2.33.1.20191209) #175 SMP PREEMPT Thu Oct 15 14:17:41 BST 2020
> [ 0.000000] Machine model: ARM Juno development board (r0)
> [..]
> [ 1.714340] mhu 2b1f0000.mhu: ARM MHU Mailbox registered
> [ 1.722768] NET: Registered protocol family 17
> [ 1.727364] 9pnet: Installing 9P2000 support
> [ 1.731689] Key type dns_resolver registered
> [ 1.735474] usb 1-1: new high-speed USB device number 2 using ehci-platform
> [ 1.736407] registered taskstats version 1
> [ 1.747061] Loading compiled-in X.509 certificates
> [ 1.755885] scpi_protocol scpi: SCP Protocol 1.2 Firmware 1.21.0 version
> [ 1.770484] cpu cpu0: EM: created perf domain
> [ 1.778505] cpu cpu1: EM: created perf domain
> [ 1.807449] scpi_clocks scpi:clocks: failed to register clock 'pxlclk'
> [ 1.897593] hub 1-1:1.0: USB hub found
> [ 1.901656] hub 1-1:1.0: 4 ports detected
> [ 2.559453] atkbd serio0: keyboard reset failed on 1c060000.kmi
> [ 22.787431] rcu: INFO: rcu_preempt detected stalls on CPUs/tasks:
> [ 22.793536] rcu: 1-...0: (1 ticks this GP) idle=222/1/0x4000000000000002 softirq=63/64 fqs=2626
> [ 22.802421] (detected by 2, t=5255 jiffies, g=-991, q=9)
> [ 22.807823] Task dump for CPU 1:
> [ 22.811049] task:swapper/1 state:R running task stack: 0 pid: 0 ppid: 1 flags:0x0000002a
> [ 22.820980] Call trace:
> [ 22.823429] __switch_to+0x138/0x198
> [ 23.583444] rcu: INFO: rcu_preempt detected expedited stalls on CPUs/tasks: { 1-... } 5443 jiffies s: 49 root: 0x2/.
> [ 23.593995] rcu: blocking rcu_node structures:
> [ 23.598449] Task dump for CPU 1:
> [ 23.601680] task:swapper/1 state:R running task stack: 0 pid: 0 ppid: 1 flags:0x0000002a
> [ 23.611619] Call trace:
> [ 23.614064] __switch_to+0x138/0x198
> [ 85.807430] rcu: INFO: rcu_preempt detected stalls on CPUs/tasks:
> [ 85.813534] rcu: 1-...0: (1 ticks this GP) idle=222/1/0x4000000000000002 softirq=63/64 fqs=10502
> [ 85.822506] (detected by 2, t=21009 jiffies, g=-991, q=9)
> [ 85.827994] Task dump for CPU 1:
> [ 85.831220] task:swapper/1 state:R running task stack: 0 pid: 0 ppid: 1 flags:0x0000002a
> [ 85.841150] Call trace:
> [ 85.843596] __switch_to+0x138/0x198
> [ 87.071446] rcu: INFO: rcu_preempt detected expedited stalls on CPUs/tasks: { 1-... } 21315 jiffies s: 49 root: 0x2/.
> [ 87.082088] rcu: blocking rcu_node structures:
> [ 87.086540] Task dump for CPU 1:
> [ 87.089773] task:swapper/1 state:R running task stack: 0 pid: 0 ppid: 1 flags:0x0000002a
> [ 87.099708] Call trace:
> [ 87.102155] __switch_to+0x138/0x198
> [ 148.827442] rcu: INFO: rcu_preempt detected stalls on CPUs/tasks:
> [ 148.833565] rcu: 1-...0: (1 ticks this GP) idle=222/1/0x4000000000000002 softirq=63/64 fqs=18377
> [ 148.842543] (detected by 4, t=36762 jiffies, g=-991, q=9)
> [ 148.848037] Task dump for CPU 1:
> [ 148.851268] task:swapper/1 state:R running task stack: 0 pid: 0 ppid: 1 flags:0x0000002a
> [ 148.861207] Call trace:
> [ 148.863663] __switch_to+0x138/0x198
> [ 150.559443] rcu: INFO: rcu_preempt detected expedited stalls on CPUs/tasks: { 1-... } 37187 jiffies s: 49 root: 0x2/.
> [ 150.570082] rcu: blocking rcu_node structures:
> [ 150.574535] Task dump for CPU 1:
> [ 150.577767] task:swapper/1 state:R running task stack: 0 pid: 0 ppid: 1 flags:0x0000002a
> [ 150.587705] Call trace:
> [ 150.590151] __switch_to+0x138/0x198
>
> - Commit working as expected:
> * 558e4c36ec9f Krzysztof Kozlowski 7 weeks ago maiblox: mediatek: Fix handling of platform_get_irq() error
>
>
> [1] https://developer.arm.com/tools-and-software/development-boards/juno-development-board
>
> Thank you,
> Ionela.
>
>> --
>> 2.25.4
>>
>>
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>> linux-amlogic@...ts.infradead.org
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